737 MAX
Incident Reports

U.S. based airlines are required to submit safety reports called Service Difficulty Reports (SDRs) for malfunctions involving aircraft systems in accordance with U.S. law. The Federal Aviation Administration (FAA) is required by Department of Transportation policy to investigate these incidents to determine root causes and to ensure corrective action is taken by aircraft manufacturers and airlines to fix the problem(s). These reports are crucial for maintaining and improving aviation safety, as they help to identify potential hazards, evaluate risks, and implement corrective measures to prevent future tragedies.

The foundation believes it is important to highlight select reports involving 737 MAX airplanes. We find the reports listed below concerning because of the history of the MAX and the repetitive and/or serious nature of the reports.

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ASAA – Alaska Airlines, AALA – American Airlines, CALA – United Airlines, SWAA – Southwest Airlines

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Control Number
CALA2024101800855
Discrepancy Date
10/16/24
Submission Date
10/18/24
Airline Name
CALA
Registry Number
57286
Aircraft Make
BOEING
Aircraft Model
7378
Aircraft Total Time (hrs)
5977
Discrepancy
LE FLAPS TRANSIT ILLUMINATED AFTER FLAP RETRACTIONSDR STARTED PER FIM 27-81 TASK 830 REPLACE THE FSEU M1746 IF ALL MESSAGE ARE NOT ACTIVE. INSTALLED NEW FSEU PER AMM 27-51-01-400-801 , COMPLETED UP TO F(1) PER AMM 27-51-01-400-801. ROTOABLE PARTS HAS BEEN COMPLETED. NEED TO COMPLETE ALL TEST PER AMM ADD EMP:U102091 27-51-01-400-801. SEE ELOTO FOR OPEN CBS. PARTS USED: 43-2751-9-0013,QTY :1 ROTABLE PARTS CHANGE WAS INDICATED - TT # 1522772 SN OFF 9004 UNIT, FLAP SLAT OFF 43-2751-9-0013 9004 ON 43-2751-9-0013 9162 AHM SHOWED FAULTS 27-81214 "LE SLAT 8 OUTBOARD SENSOR SIGANL DOES NOT AGREE WITH OTHER LE SLAT OUTBOARD SENSOR SIGNALS" AND 27-81215 "LE SLAT 8 INBOARD SENSOR SIGNAL DOES NOT AGREE WITH OTHER LE SLAT INBOARD SIGNALS" FSEU REPLACMENT WAS NO HELP WHILE PERFORMED A LEADING EDGE CRUISE DEPRESSURIZATION TEST IN REFERENCE TO B737 AMM 27-81-00-730-801 NOTICED THE NUMBER 8 SLAT LAGGED BEHIND THE REST OF THE SLATS ON EXTENTION DURING TEST WHEN SLAT WHERE RETRACTED NUMBER 8 SLAT RETRACTED QUICKER THE THE REST AND SLATS LOCKED OUT DUE TO ASSYMETREY MAINT LIGHT ILLUMINATED AND AND BOTH SMYDS SHOWED MESSAGES FOR LEADING EDGE SLAT ASYM SUSPECT NUMBER 8 SLAT ACTUATOR OR RIG REFERENCE B737 FIM 27-81 TASK 820 ADDED PICTURES OF DIFFERENCE BETWEEN NUMBER 7 AND 8 SLAT AS WELL AS NUMBER 1 AND 2 SLAT ON THE OPPPOSITE WING FOR COMPARISON AFTER VERIFIED #8 SLAT ACTUATOR ROD END TORQUE AND FINAL INSTALLATIONLEAK CK AND OPERATION OF #8 SLAT, NO LIMITING DEFECTS NOTED PER GMM 09-10-05
Control Number
CALA2024101700853
Discrepancy Date
10/15/24
Submission Date
10/17/24
Airline Name
CALA
Registry Number
17289
Aircraft Make
BOEING
Aircraft Model
7378
Aircraft Total Time (hrs)
5566
Discrepancy
CB FOR FWD GALLEY COFFEE MAKER POPPED WAS NOT IN USE MAKER NUMBE R 105REMOVED C/M 105 AND C/M 106. INSPECTED VISIBLE WIRING, CONNECTORS, GROUNDS FOR SHORTS OR DEFECTS, NONE NOTED. REMOVED POWER PANEL ASSY IN FWD GALLEY NEXT TO C/MAKERS. INSPECTED WIRING, CONNECTORS AND CLAPS FOR DAMAGE OR SHORTS, NO DEFECTS NOTED. REMOVED POWER PANEL NEXT TO FORWARD OVEN. INSPECTED WIRING, CONNECTOR AND GROUNDS. NO DEFECTS NOTED. OPERATED BOTH FORWARD OVENS FOR 20 MINUTES, NO DEFECTS. CONTINUED... RAN SEVERAL BREW CYCLES ON BOTH FWD C/MAKERS. NO DEFECTS. VERIFIED BOTH HOTPLATE DRAINS DRAIN PROPERLY. CREW REPORTED THAT INTO PBI THE PRIOR FLIGHT, THEY NOTICED AN ELECTRICAL SMELL BUT NO SMELL WAS IN GALLEY. SUSPECT POSSIBLE SHORT OR DEFECT BETWEEN FWD GALLEY POWER SOURCE AND THE 2 FORWARD GALLEY MODULES. NEEDS FURTHER TROUBLESHOOTING TO DETERMINE CAUSE. T/S PER WDM 25-31-11 AND CMM 25-31-147. FOUND LOOSE SCREWS ON TERMINAL LUGS OF CB101 AND CB102. TIGHTENED SCREWS. MEASURED CURRENT ON ALL 3 PHASES WITH CLAMP METER. MEASURED 0 AMPS WITH BOTH COFFEE MAKERS AT REST AND 6.6 AMPS FOR EACH COFFEE MAKERS WHEN THEY WERE BREWING. ISOLATED CIRCUIT BY PULLING CB C914 AND REMOVING GALLEY PWR IND LIGHT. MEGGED WIRES AT RECEPTACLES OF COFFEE MAKERS 105 & 106. EACH PHASES TO NEUTURAL AND GND & TO EACH OTHER. NON DEFECTS NOTED. RE-INSTALLED ALL BACK TO THEIR ORIGINAL POSIPOSITIONS. PERFORMED OPS CHECK OF COFFEE MAKERS 105 & 106 IAW AMM 25-32-01. OPS CHECK GOOD. CB102 AND CB103 REMAINED IN AFTER NUMUROUS TESTS.
Control Number
CALA2024101400832
Discrepancy Date
10/12/24
Submission Date
10/14/24
Airline Name
CALA
Registry Number
37521
Aircraft Make
BOEING
Aircraft Model
7379
Aircraft Total Time (hrs)
12638
Discrepancy
STRONG ELEC SMELL IN CABIN ROWS 22-27 QRH RAN AT FL350 THEN DI VERT TO DENFLIGHT AND CABIN CREWS COMPLIED WITH SMOKE ODOR QUESTIONAIRE SEE PICS FIM 21-00- TASK 830 NEEDS COMPLIED WITH REMOVED AND REPLACED RELAY R560 REF SWPM 20-81-11 AND AIPC 24-21-21-61A. REMOVED CEILING PANELS AROUND ROWS 21-27, NO DEFECTS NOTED IN ANY WIRING. INSTALLED CEILING PANELS PER AMM 25-21-45. TURNED ON PED OUTLETS AND PLUGGED INTO SEVERAL, NO SMELL COMING FROM ANY OUTLETS. TURNED ON BOTH LEFT AND RIGHT PACKS, SET EACH TEMPERATURE CONTROL TO COLD, NO SMELL. SET TEMP TO AUTO, NOTICED HEAVY ELECTRICAL/BURNING SMELL IN ROWS 21-27. PER FIM 21-00 TASK 830 STEP Q(3) INSPECTED AIR RECIRC FAN FILTERS. BOTH FANS AIR FILTERS SMELLED OF BURNING SIMILAR TO CABIN. REPLACED LEFT AND RIGHT AIR RECIRC FANS FILTERS PER AMM 21-25-01-400-801. PARTS USED: 29-2124-3-0006,QTY :1 OPERATED BOTH PACKS ON AUTO TEMP FOR 10 MINUTES. SMELL IN CABIN IS LESS BUT STILL PRESENT IN SAME ROWS. REMOVED AND REPLACED LEFT RECIRCULATION FAN. AMM 21-25-03-400-801. UP TO AND INCLUDING, STEP 3. C. (2) (A). STILL REQUIRES LEAK CHECK. PARTS USED: 29-2125-9-0001,QTY :1 ROTABLE PARTS CHANGE WAS INDICATED - TT # 1368631 SN OFF 7825 FAN, AIR, DISTR OFF 29-2125-9-0001 7825 ON 29-2125-9-0001 4365 REMOVED & REPLACED RIGHT RECIRC FANREF AMM 21-25-03-400-801 UP TO AND INCLUDING STEP 3. C. (2) REF FIM 21-00 TASK 830. REPLACED BOTH L/R RECERT FANS PERCATIONAATY. PACKS RUNNING,FANS RUNNING, UNABLE TO DUPLICATE ELCT SMELL. ADD EMP:U411446
Control Number
CALA2024091100620
Discrepancy Date
9/10/24
Submission Date
9/11/24
Airline Name
CALA
Registry Number
37562
Aircraft Make
BOEING
Aircraft Model
7379
Aircraft Total Time (hrs)
4440
Discrepancy
ROLL AUTHORITY ON FINAL 7NM 1500FT PER DFCS BITE SEE PHOTOS. REF AMM 22-11-00 PER FIM 22-11 TASK D79. PER AMM22-11-25-710-801 TEST PASS NO FAULTS . ADD EMP:U102168 NEED TO CONTINUE WITH FIM 22-11-D79. PERFORMED AMM 27-11-00-710-801, OPS CHECK IS GOOD. PERFORMED AMM 27-61-00-710-801, OPS CHECK IS GOOD. BOTH REQUIRED PER FIM 22-11 D 79. AMM TASKS 22-11-25-710-801, 22-23-00-710-802, 27-11-00-730-801, 27-21-00-700-805 & 27-21-00-700-807 STILL NEED TO BE ACCOMPLISHED PER FIM 22-11 D 79. ATTEMPTED TO PERFORM LAND VERIFY TEST TO NARROW DOWN TROUBLESHOOTING. ACFT IS FAILING DUAL STAB AND SUBSEQUENTLY MACH TRIM TESTS AND GIVING HARD FAULT OF 22-11191 MT CMD MON. ADDING FCC PART PRECAUTIONARY. ABOVE UPDATE FOR MESSAGE 22-11191 TRANSCRIBED TO LOGPAGE 9215536 SEE REFERENCED LOGPAGE FOR DISPOSITION PERFORMED AUTOPILOT AILERON ACTUATOR TEST IN REFERENCE TO B737 AMM 22-11-25-710-801 TEST PASSED PERFORMED YAW DAMPER SYSTEM TEST IN REFERENCE TO B737 AMM 22-23-00-710-802 SYSTEM TEST PASSED UPDATED FOR SDR PERFORMED AILERON TRIM RESPONSE TEST IN REFERENCE TO B737 AMM 27-11-00-730-801 TEST PASSED ADD EMP:U388284, PERFORMED RUDDER TRIM SYSTEM TEST IN REFERENCE TO B737 AMM 27-21-00-700-807 TEST PASSED PERFORMED RUDDER TRAVEL TEST IN REFERENCE TO B737 AMM 27-21-00-700-805 TEST PASSED ALL TESTS IN B737 FIM 22-11 TASK D79 HAVE BEEN COMPLETED WITH NO FAULTS FOUND ADD EMP:U388284, COMPLETED B737 FIM 22-11-D79 WITH NO FAULTS FOUND SPOKE WITH TOMC OK TO CLEAR FCC A REPLACED ON LOGPAGE 9204147
Control Number
CALA2024090600578
Discrepancy Date
9/4/24
Submission Date
9/6/24
Airline Name
CALA
Registry Number
27292
Aircraft Make
BOEING
Aircraft Model
7378
Aircraft Total Time (hrs)
6079
Discrepancy
STAB TRIM UNCOMMANDED NOSE DOWN TRIM DURING LANDING ROLLOUT. MAI N ELEC TRIM NOT APPLIEDTALKED TO PILOTS. STAB ON LAND ROLLOUT WITH AUTO PILOT OFF TRIM STARTED TO GO FULL DOWN. PILOT MADE SURE HAND WAS OFF ELECTRIC TRIM. WHEN NOTICED WAS OFF THEY HOT TRIM CUT OUT AMD THE TRIM STOPPED. NO FUALTS IN HISTORY AND NO FULTS IN EXSITING OR INBOUND. UPDATED TO REPORT SDR FOUND NO FAULTS IN INBOUND FLIGHT DECK EFFECTS OR FAULT HISTORY PEROFORMED STABALIZER TRIM MOTOR TEST IN REFERENCE TO B737 AMM 27-41-71-700-801 TEST PASSED AWAITING ESC TO REVIEW QAR DATA FOR FURTHER DIRECTION PERFORMED DIGITAL FLIGHT CONTROL SYSTEM SPEED TRIM/STAB TRIM DISCRETE BITE TEST IN REFERENCE TO B737 AMM 22-11-00-740-815 TEST PASSED STILL AWAITING ESC RESPONSE FOR FURTHER DIRECTION AFTER QAR DATA REVIEW VERIFIED BOTH FCC'S IN GROUND MODE 28 VOLTS ON BOTH FCC A AND B ON PIN B3. PER ESC REQUEST PERFORMED AN ANGLE OF ATTACK SENSOR SYSTEM TEST IN REFERENCE TO B737 AMM 34-21-05-730-801 TEST PASSED PERFORMED DFCS BITE FOR THE ADIRU AND SMYD IN REFERENCE TO B737 AMM 22-11-00-740-801 TEST PASSED PERFORMED AN OPERATIONAL TEST OF THE STALL WARNING SYSTEM IN REFERENCE TO B737 AMM 27-32-00-710-802 OPERATIONAL TEST PASSED NO FAULTS FOUND CONFIRMED BOTH FCCS INSTALLED ARE 822-1604-102 REFERENCE B737 IPC 22-11-33-03 AS REQUESTED REPLACED FCC A IN REFERENCE TO B737 AMM 22-11-33-400-801 CONFIRMED CORRECT SOFTALL ABOVE ACTIONS COMPLIED WITH PER ESC INSTRUCTIONS. REPLACED BOTH FCCS ALL OPERATIONAL TESTS PASSED OK TO CLOSE ITEM
Control Number
CALA2024090500561
Discrepancy Date
9/4/24
Submission Date
9/5/24
Airline Name
CALA
Registry Number
37528
Aircraft Make
BOEING
Aircraft Model
7379
Aircraft Total Time (hrs)
12266
Discrepancy
PER INBOUND CAPTAIN, AT ALTITUDE IN CRUISE, EXPERIENCED UN COMMANDED ROLL RIGHT. MAX ROLL AUTHORITY LIMIT STOP WAS REACHED. AIRCRAFT WAS AT FL 340, 255KTS ON ARRIVAL. THEY WERE APPROACHING A WAYPOINT THAT REQUIRED A SLIGHT RT TURN. AUTOPILOT STARTED THE RIGHT TURN AND CONTINUED UNTIL AIRCRAFT REACHED 33 DEGREES OF BANK. THE AUTOPILOT THEN COMMANDED YOKE TO LEFT TO CORRECT BUT THE PLANE CONTINUED TURNING RIGHT. AT THIS POINT "ROLL AUTHORITY" WAS ANNUCIATED. PILOTS THEM DISCONNECTED AUTOPILOT AND MADE EXCESSIVE LEFT ON YOKE TO REGAIN WINGS LEVEL. PILOTS STATED THEY EXPERIENCED BUFFETING/SHUDDERING THROUGH THE AIRFRAME. THEY STATED IT SEEMED LIKE A SPOLIER WAS UP. THEY DONT THINK IT WAS WAKE TURBULENCE OR MOUNTAIN WAVE TURBULENCE. ACCESSED MY BOEING FLEET TO FIND MAINTENANCE MESSAGES. NONE FOUND. ACCOMPLISHED SEVERE OR UNUSUAL TURBULENCE, EXCESSIVE MANEUVER CONDITIONAL INSPECTION ON LOG PAGE 9133363 FOLLOWED FIM 22-11 TASK D79. PREFORMED ALL OPS CHECKS LISTED. ALL OPS CHECKS GOOD, FOUND NO DISCREPANCIES. ACCOMPLISHED DFCS BITE TESTS REF AMM 22-11-00-740-814 AND LAND VERIFY TEST PASSED. HOWEVER A RELATED FAULT WAS FOUND IN LEG 01. FAULT MSG 22-11715, "ROLL AUTHORITY" MATCHES THE DATE AND FLIGHT PARAMETERS. NEED TO ACCOMPLISH FIM TASK 22-11 TDUE TO UNCOMMANDED ROLE WE HAVE C/W FIM TASK 22-11-C37, AND 22-11-D79. REF LOG PAGE 9133363 FOR SEVER TURBULANCE INSPECTION C/W. A/C HAS BEEN RETURNED TO SERVICE AND READY FOR T-HOP.
Control Number
CALA2024080800393
Discrepancy Date
8/6/24
Submission Date
8/8/24
Airline Name
CALA
Registry Number
17337
Aircraft Make
BOEING
Aircraft Model
7378
Aircraft Total Time (hrs)
2001
Discrepancy
LE FLAP TRANSIT LIGHT ILLUMINATED IN FLIGHT - DID NOT RESET AFTE R QRH PROCEDUREBEGAN TROUBESHOOTING PROCEDURE. FAULT SHOWS ON #1 LEADING EDGE FLAP WITH ASSOCIATED MTC MESSAGE 27-81216. UNABLE TO CLEAR FAULT THROUGH FSEU INTERROGATION. REF FIM TASK 27-81 822. FAULT REMAINS. PERFORMED UP TO STEP D3 (FSEU REPLACEMENT) WHILE INSPECTING LE FLAP RETRACT SENSOR 1, FOUND SPLICES HAD SLIGHTLY PULLED APART DUE TO WIRE BUNDLE SECURED TOO TIGHTLY. SUSPECT THAT COULD BE POSSIBLE ISSUE. REMOVED AND RESPLICED WIRES FOR LE FLAP RETRACT SENSOR 1 (S168) REF SWPM 20-30-12. DURING TESTING IT WAS A NO FIX. LEFT LE FLAP 1 IN TRANSIT LIGHT STILL ILLUMINATED AND FAULT STILL EXISTS. MAY NEED NEW FSEU OR FURTHER WIRING CHECKS ACCOMPLISHED. SUSPECT SWITCH S-168 IS BAD, MOVED FLAPS TO A POSITION WHERE ALL SENSORS WERE OFF THEIR TARGETS, USED A SCALE ON OTHER 3 RETRACT SENSORS TO SIMULATE THE TARGET, ALL THEIR RESPECTIVE LIGHTS WENT OUT, DID THE SAME THING TO S -168 NO CHANGE STILL SHOWED IN TRANSIT. REMOVED LE FLAP 1 RETRACT SENSOR S168 REF AMM 27-88-11/401, RESISTANCE CKS OF WIRES FROM S168 TO THE FSEU GOOD REF WDM 27-81-11-1, INSTALLED NEW SENSOR S168 NO FIX, T/S FURTHER AND FOUND BAD GROUND AT GD614AC. VERIFIED GROUND GD614-AC IS BAD. BRACKET NOT GROUNDED TO THE AC. PERFORMED WIRING CHECKS FROM SWITCH S168, TO. FSEU REF WDM 27-81-11, SWITCH CHECKS GOOD. REBITE CK OF FSEU GOOD IAW AMM 27-51-01/401.